Analisis Redesain Fasilitas Produksi Departemen Pewarnaan Guna Meminimalisir Biaya Material Handling pada PT. Surya Pertiwi Nusantara
DOI:

Abstract
Factory layout is a facility design that aims to facilitate efficient material movement and optimal utilisation of production areas. PT. Surya Pertiwi Nusantara is a company engaged in the manufacture of sanitary ware. Based on observations in the colouring department, there are problems with the material transfer process, namely the distance between work stations is quite far, which has an impact on travel time. This results in wasteful material handling costs. Data processing was carried out using the From To Chart method and Activity Relationship Chart. The results of the research using the From To Chart method produced an alternative layout with a material handling moment of 7,814. 342.8 metres/month and OMH of Rp. 940,846,873.1/month, compared to the initial layout, which had a material handling moment of 18,334,175.2 metres/month and OMH of Rp. 1,078,049,501.8/month. Based on these results, the layout alternative using the From To Chart method was chosen.
Downloads
References
Wignjosoebroto S. Tata letak pabrik dan pemindahan bahan. 3rd ed. Jakarta: PT Guna Widya; 1996.
Simanjuntak RA, Asih EW, Winardi F. Usulan perbaikan tata letak fasilitas produksi kayu olahan menggunakan metode activity relationship chart, CRAFT dan from to chart. Pros SNAST. 2022 Nov;:10–7.
Purnomo H. Perencanaan & perancangan fasilitas. 1st ed. Yogyakarta: Graha Ilmu; 2004.
Hadiguna RA, Setiawan H. Tata letak pabrik. Ed. 1. Yogyakarta: C.V. Andi Offset; 2008.
Santoso, Heryanto RM. Perancangan tata letak fasilitas. 1st ed. Bandung: Alfabeta; 2020.
Hartini TS, Atikah. Desain tata letak gudang untuk meminimalkan ongkos material handling pada PT Rotaryana Prima. 2023;5.
Amaria AN, Purnama J, Taniharjo MB. Perancangan tata letak fasilitas untuk menurunkan ongkos material handling di PT Suna Dwi Tunggal Perkasa. 2023;:29–38.
Fitranto SF, Murnawan DH. Usulan perancangan ulang tata letak fasilitas guna meminimalisir jarak material handling. Surabaya Jl. Semolowaru No. 2022;45(Arif 2017):1–11.
Jamalludin, Fauzi A, Ramadhan H. Metode activity relationship chart (ARC) untuk analisis perencanaan tata letak fasilitas pada Bengkel Nusantara Depok. Bull Appl Ind Eng Theory. 2020;1(2):20–2.
Soerijayudha MW, Rahayu D. Perancangan ulang tata letak fasilitas pada PT Kharisma Plastik Indo. J Rekayasa dan Optimasi Sist Ind. 2021;3(1):32–9. Available from: http://journal.univpancasila.ac.id/index.php/jrosi/article/view/2489
Muharni Y, Febianti E, Vahlevi IR. Perancangan tata letak fasilitas gudang pada Hot Strip Mill menggunakan metode activity relationship chart dan blocplan. J Has Penelit dan Karya Ilm dalam Bid Tek Ind. 2022;8(1):44–51.
Aulia B, et al. Analisis tata letak fasilitas Toko Prima Freshmart SV IPB melalui metode activity relationship chart (ARC) dan total closeness rating (TCR). J Teknol dan Manaj Ind Terap. 2023;2(2):128–34. https://doi.org/10.55826/tmit.v2i2.155
Amaria AN, Miraningsih YM, Putri VA, Julyandini YC, Murnawan H. Usulan rancangan tata letak fasilitas dengan menggunakan metode from to chart (Studi kasus: UD Karya Abadi). J Sustain Ergon Optim Appl Ind Eng. 2022;4(2):115–23.
Hasanah N, Utami FT, Fauzan MHN, Kristyanto DH. Implementasi material handling dalam mencari jarak dan ongkos material serta usulan tata letak produksi di PT Wijaya Karya Beton. Tek Ind. 2022;3(1):29–33.
Downloads
Published
How to Cite
Issue
Section
License
Copyright (c) 2025 Arnoldus Ivan Bagus, Jaka Purnama

This work is licensed under a Creative Commons Attribution-NonCommercial-ShareAlike 4.0 International License.